Initial Check2006-02-04
Engine arrived stripped with most smaller components boxed. Crankshaft in good condition, one big-end bearing showed signs of break up.
Strip and Inspection
2009-04-18
Crank removed and found to be in good order. Number 3 big-end U/S with a large piece broken out of the top half.
Pistons removed, bores 1 and 2 in good condition having been chromed at some point. Number 3 liner in poor condition. All three pistons have stuck rings with several broken. All three gudgeon pins require refurbishment.
Installation
2010-02-19
Block/crank/flyhweel/outrigger back together. Deflection less than 1 thou all round.
Ongoing work
2011-07-23
Remaining two flywheel bolts fitted and injection pumps set (by eye)
Knock on No 3 so big ends checked.
Big End Clearances
Cylinder | Initial | Current |
1 | 0.004" | 0.004" |
2 | 0.004" | 0.004" |
3 | 0.009" | 0.004" |
Further Work
2011-10-30
Inlet and exhaust valves removed and ground, new water seals fitted on exhaust valves.
General sorting of remaining small jobs, missing studs, fuel leak on manifold.
Still needed, investigation of possible leak in oil cooler following fresh water found in sump.
End of Season/Victorian Night/NYD 2011
2012-01-03
Cooling system pressurised with no leaks. Engine ran for 2.5 hours at Victorian Night. Ran for 5 hours at New Years Day event with no problems other than hunting on the governor. 5 gallons of fuel consumed.
Circ Pump Failure
2013-06-08
Circulating pump failed so the engine is currently U/S.